Up to date information regarding the restoration of steam locomotive 6029 in Canberra, ACT Australia. Beyer Garratt 6029 is an EX NSWGR locomotive and was a member of the largest, and most powerful class in Australia. The restoration to full working order is being undertaken by volunteers in Canberra.
6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Nov 4, 2012
Super Week November 2012
Super week started early Monday morning with the usual cup of tea and a chat. It was pleasing to see some of the old faces and even some newcomers.
The first job for the day was to move 6029 out of the shed as this would allow the fork lift close unrestricted access to the locomotive. The team spent a good hour cleaning and oiling up 6029 to ensure a trouble free shunt. Diesel locomotive D25 was fired up and with little effort, 6029 moved gracefully out of the shed. The team was delighted to see the motion and valve gear rotating and oscillating as it should...a tribute to all who were involved.
Once outside, the power reverser mounting bracket was lifted and attached on the driver’s side of the boiler. Next the power reverser itself but it was soon realized that the centre actuating lever would have to be fitted first, so the reverser was lifted off to fit the lever. Back on again and with some gentle alignment the assembly was soon complete. It took some time to find the pins that connect the actuating lever to push and pull rods (being a Garratt is goes both ways). Once found in the store all was well, a after a quick clean-up, and a few drops of oil, the pins fitted snugly into place. These pins must be a good fit with only minimal clearance as any lost motion would compromise the valve setting and the operating efficiency of the valve gear. Believe it or not this is the first stage of the all-important valve setting. The first step is to establish true mid gear from the reverser down to the expansion links x 4. Again no lost motion is allowed in all pins and bushes. After a quick check it was confirmed that all was well.
The smoke stack was assembled along with the petticoat pipe however this whole assembly was too big for our forklift and a crane contractor was called in to complete the lift onto and into the smoke box. Once lowered into place, the alignment of the smoke stack to the blast pipe was checked and some extra work will be required to complete this task in the future.
The main steam pipe that delivers live steam from the smokebox to the hind unit was lagged and both lens rings that join the pipe at either end were given a final lap. The finished pipe assembly was fitted into place on the outside of the boiler cradle. This pipe is connected to an expansion section that includes a sliding joint. This section has been in storage for a few years and once located it was stripped for a final paint in all over basic black.
The stoker feed screw and delivery sections were next on the list for attention. The stoker trough was set up on stands to facilitate cutting out the worn through sections with new sections. It was soon realized that all was not well and the further the job progressed, the more rust was found. The obvious decision was to cut out the trough and replace it with new. The castings will be kept including the reduction gear box that makes up the trailing end. Every rivet was cut off and punched out with the sledge hammer.
The remaining castings were cleaned up in preparation for painting. The gear box was eventually stripped down with a bucket load of black gummy grease oozing out once the rear cover was removed. The state of the grease indicate that this gear box has not been cleaned out for many years however it has done its job as the gear train is in good condition. Many of the parts will be washed clean and reassembled as time permits. A new stoker trough will be sourced and once on site the stoker trough will be re assembled.
Saturday was dedicated to a site clean-up and a general go slow as the team was feeling the effects on working six days straight. Oh well back to the office next Monday.
Oct 16, 2012
6 and 7 October 2012
The cab work continued with the fitting of the windows to the cab side doors. Safety glass has been ordered for the leading windows including the two round port holes that the NSWGR blanked off many years ago. The re en-statement of these windows is part of the overall plan to out shop 6029 in its 1950's configuration as far as practicable.
On Sunday work commenced on the fit out of the smoke box with the installation of the blast pipe. With the blast pipe fitted the next job will be to fit the smoke stack aligned and secured home. The steam pipes and elbows that deliver steam from the super heater header to the the cylinders were taken out of storage ready for fitting. These pipes are bolted together with convex lenz rings that allow for any mis-alignment. The rings will have to be lapped in by hand and we are looking for volunteers who have the willingness and patience to complete this vital task.
Sep 14, 2012
An overview of work to date
After five years of toil through freezing winters and hot summer heat waves we are now at a point where we are now have to consider how we will operate 6029. From the teams perspective we have to actually pinch ourselves as we have come so far from that first workday in August 2007.
6029 now resides in the museums large shed in preparation of the final paint job over summer. The myriad of smaller components that have been stored, ready for use, are now seeing the light as they are fitted on to the locomotive proper.
The leading tank is now in place and the valve gear on the leading engine unit is almost done and dusted.
Our last workday involved the laying out of the pipe work for the smoke box including the blast pipe with all of the small bore pipe work.
The off-site teams have now almost completed the rebuild of the stoker motor and power reversing gear.
This all means that yes, we are heading in the right direction towards throwing that first match in the firebox.
Having said all that we need your help now both financially and with man power. Our workdays are now held every Saturday. If you would like to donate to our appeal, all donations are tax deductible.
2013 is now shaping up to be the year of 6029 and yes you are most welcome to join us for the ride.
Alan Gardner
1 September 2012
continued with the fitting of the coupling rod. As this rod is very
heavy, a chain block was used to lift it into position. This task is
not easy and requires a specific sequence to be followed as the crew
found out. Yes you can fit the roller bearing around the wrong way
and no, you cant fit the tapered sleeve to match.
The 18 fitted bolts that secure the front tank to the main frame were
taken out of storage and cleaned up with the wire brush. These bolt
assemblies are unique as the are fitted with a spring that the
prevents the nuts loosening off. Having said that it also makes is
hard to fit. The crew still had to make more timber packing to
fits between the tank and the main frame, so it was off to the timber
store to find some hard wood.
The cab timber lining received another coat of clear varnish and the
support strapping was painted in gloss black The next work day should
see all the roof work finished and with this done, the electrical
conduit will be next.
Our workdays are now held every Saturday and as the weather is now
warning up we are planing to hold a super week in October
(accommodation available). Date to be advised.
Alan Gardner
Jul 25, 2012
Sunday 15 July 2012
Once in position the team took the optionality to pose for the camera and it was pleasing to see the locomotive basking in the sun. The front tank was carefully lowered into place by a specialist crane contractor and again, there was a slight pause for the cameras. The crane was utilised to remove the hind bunker to facilitate the next stage in the rebuild program.
D25 pushed 6029 back into the shed just in time for lunch. After a good feed the crew jumped back into the fitting of the leading coupling and connecting rods. The valve gear re-work continued with the team progressing well with the polishing and re-fit.
The overall work plan is to continue with the fitting of all the motion components (coupling, connecting, valve gear) and with the rear bunker now out of the way, the hind lubrication system.
The hind bunker stoker motor system including the screw trough will be the next major task in the coming months. Significantly this represents the last of the of the major rebuilds and once completed the hind bunker will be lowered back into place.
The obvious question is when will the steam trials start. To keep a long story short, its basically up to our ability to raise funds and the continued support of our volunteer work force. In real terms we are about 80% through the project and if we can increase our volunteer work force with just a few more regulars we will be lighting the first match later this year. If you haven't been on site for a while or even if you are a new face you will be most welcome.
Work days are now every Saturday and the third Sunday of every month.
Jun 25, 2012
Weekly Progressions
Jun 18, 2012
Sunday 17 June 2012
The installation of the coupling and connecting rods continued on the right hand leading engine unit. These components were originally crack tested and assessed a few years back and while in storage, had developed the usual layer of surface rust. This was easily was polished off while the locking split pins were fitted to the castellated lock nuts on the coupling rods before the team turned its attention the largest component being the connecting rod. This is a one piece forging that is over ten feet long. The roller bearing was given one last clean out and inspection, then after an initial team meeting (how are we going to do this), the rod was fitted into place. As the rod is very heavy, and we are undercover and without any form of crane, a system of rollers and levers were deployed. To the teams amazement, this task was completed with relative ease. It seems that Mr. Isaac Newton actually did know a thing or two, and not sleeping through the all those physics lectures many years ago actually paid off. Thanks to David, Tony and Patrick for the elbow grease used to polishing the rods. Only three sets to go boys!
Back over in the cab, Andy continued with the fitting of the timber roof lining. This job has to be completed before the electrical conduits can be fully fitted, but more importantly, completion will allow the fitting of the whistle cords. Andy has been working on this job between workdays and estimates that it will be completed in the next month.
Ian and his team have also been working in the cab area, but in this case it’s all under the floor. The myriad of pipes and valves that control the stoker motor continue to be fitted, all be it with continued reference to the original drawings. Ian has copied the pipe drawing and used colored pencils to sort out what goes where.
The front tank is almost ready for the vital water test with only a blanking plate to be fitted in place . This job will have to be done in the mid-afternoon the allow ice to thaw... It is, after all, the middle of winter here.
Alan Gardner
Jun 5, 2012
Saturday 2 June 2012
The 6029 management team recently met to review the project plan against the original Gantt chart. In general terms we are tracking well, and the large inventory of stripped components is reducing in size as they are progressively refitted to the locomotive. It is estimated that about 10% of the inventory is still to be fitted, however this means the 90% is fitted ready for operation. From a personal perspective, I am delighted with the high standard of work that the team has achieved, and a testament to this can be seen in the photos posted every month. Some recent examples have been the Nathan mechanical lubricators, the air compressor and now the stoker motor. All have been completely stripped down to the last nut and bolt and been rebuilt better than new using the best materials available and to the highest possible standard. Another pleasing fact is that as the team rebuilds these sub-assemblies they are in fact becoming content experts on steam technology of the 1950’s. This expertise means that the end product that we are now realizing is something that the team can be very proud of.
Our extended network of help, led by our friends at Goodwin Alco has also helped the project significantly. The cab now looks as good as new, infact 80% of the cabs sheets are new, including the seats, new timber window frames and safety glass. The roof is presently being re-lined with cedar boards and yes, once again with help from Goodwin Alco.
The main focus of work in the winter months will be the fitting of the coupling and connecting rods followed soon after by the valve gear. Again the team is becoming very proficient at fitting the components of steam technology. However the fitting of the forged connecting rods will be facilitated with the use of contemporary lifting equipment.
We are now at a stage where the obvious question is being asked, when will 6029 be back in steam? Putting aside an end date guestimate, the answer will be in a review of what we still have to complete. That Gantt chart still lists the ash pan, boiler cladding sheets, smoke box, steam piping, electrical system and the stoker trough, not to mention all of the small bore copper piping that is required to complete the brake system.
The big news is that we will be holding another super week on a date yet to be advised. For those who don’t know, we take a holiday from our day jobs to spend a full week working on 6029. A bit of a conundrum for the project manager, as he has now been appointed the museums general manager full time.
Regards
Alan Gardner
May 22, 2012
The coupling and connecting rods have been crack tested and the polishing is realising good results. The driving wheels have been lined up and the locomotive was moved forward for about four feet to facilitate the best position for the eventual fitting of the coupling rods.The valve gear fit out is progressing, but we will need more willing hands to help progress what could be called arduous work.
The cab fit out is gaining momentum with a small team lead by our resident expert, Ian. The myriad of steam and air pipes are slowly going back together and the pile of stored pipes is getting smaller every workday. Graeme has worked out the best way to refit the control valves for the air compressor and the blower control with the fitting of the spindles (20 foot long) that run from the cab thought the boiler hand rail connecting to the vales attached at the smoke box end.
Our next workday is Saturday 2 June all welcome. Winter woollies will be essential.
Alan Gardner
Apr 24, 2012
Quiet Progress
If you have been following the blog for a while, you may remember the quality of the work he did on the mechanical lubricators , and it comes as no surprise that his next restoration task is being carried out to the same standard. Ian, and Glenn Bridgart have been hard at work on the stoker motor and Cardew valves, all of which have suffered from the years in service and years in open storage.
The Cardew valves, used to prevent damage from any excess water in the cylinders, being mostly brass, have suffered very little and look a treat now that they are clean, but the springs inside them are a different story and may require replacement before too long.
The stoker motor is also getting the royal treatment and while it is complete, and was not seized by exposure, is going to need a little work to set it right. The crank will need to have the journals chrome plated to repair some pitting and the piston rods will likely get the same treatment. Otherwise it has cleaned up very well and no doubt will give sterling service when it is finished.
A little work has been done on the front tank, and another day or so should see its underside completed and ready to fit. One badly corroded area of the floor will have to be replaced, but better now than when it is full of water and on the loco. David slaved away for hours removing the years of grease and grime that had accumulated under the tank, with a fair bit of elbow grease and some determination. Well done, its not the most glamorous job, but it still needs to be done.
Last but not least, there are a few images this monthof 3016 leaving Goulburn roundhouse after the maintenance work had been completed nearby.
Remember that the next workday is Saturday the 5th of May at the Canberra Museum, jobs for everyone and if your lucky, a BBQ lunch as well
Mike Reynell