6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Jul 12, 2009
Monday morning 7:30 am -4 degrees. The first job as the highest priority was to light the fire. In fact this would be repeated every morning.
As planned the boiler cradle strip down was completed and the usual undercoat and two top coats of black were applied. The reversing gear was completely seized and the rollers that facilitate easy movement had in fact worn flat when the locomotive was in operation. A compete new set of rollers is being manufactured. The pivot centre oil lines and boxes were repaired and fitted ready for use. The re fit steam delivery pipes from the smoke box to the hind unit started, however we have to order a new set of inch BSW studs and nuts to complete the job. Thanks to the efforts of Mike Ridley, Peter Gleeson, Stuart Edwards, Barry Peffer and Roger Maynard.
On the engine unit side the first of the four bogies was completely stripped down to the last nut and bolt. The lessens learnt here is that even the sub assemblies are heavy. The bogie frame was cleaned down and crack tested with no significant issues found. Three of the manganese horn liners will be replaced due to cracking in the corners. The many smaller components were progressively stripped cleaned and assessed. As previously reported the lateral control springs are in poor condition and by weeks end they were dispatched to Sydney for rebuild. Thanks to Ian Senini, Malcolm Cluett and David Griffiths.
In all 290 hours of work was completed for the week realising another significant milestone. Thanks to the efforts of all involved the boiler cradle is now almost compete. We can now move onto the overhaul of the four bogies and when completed reassembly of the locomotive proper will commence. In parallel the bogie work we will continue with the strip down of the motion and the assessment of the engine units.
We are now at what can be called the turning point of the project, however as is always the biggest threat to the project is money. We now have some big ticket items that will have to be competed in the next six months. These are,
· 20 off super heater elements. $27,000.
· Hard chroming of piston and valve rods.$ 12,000.
· Spring repairs and rebuilds. $10,000.
· Piston rings for vales, cylinders and air compressor . $14,000.
· Sundries. $20,000.
So now for the big news, if we realise the above $89,000 6029 will be steaming in 2011. We have the team and the skills to do the job, so it all gets down to money, its as simple as that. So please keep the donations coming in, no matter how small every bit counts. Collectively we can once again see Australia’s largest stem locomotive gracing the rail network.
Jul 6, 2009
Saturday 4 July Workday
Report from Peter Reynell
Another successful day, made the more memorable because it was the 33rd anniversary of the Garratt’s first trip under ARHS ACT Accreditation. And we had a little party to celebrate. Lindsay Richmond [another survivor of those early days] and I reminisced over some slides [yes, even a projector was used!] and about 25 people from the various work parties on site were shown the good old days and a good time…our ARHS on train catering crew including Chris S and Lindy S put on a much better than usual spread. Imagine Roast Beef, Oven baked Chicken fillet, party pies and salad , as well as hot doggies; sausages and all the accomaniements.And even cake!
Thanks, crew, you did us proud.
A special thanks to Brian Nye, Chief Executive of the Australasian Railway Association for coming along to offer some very encouraging words.
Oh, and we did some work too..ends were rescued from the old superheater elements, more black paint went on the boiler cradle and Paul Quinn lit a huge fire under the engine unit which eventually liberated the very frozen solid pony truck bearing which caused the angst months ago when the pony truck came off the rails. A long overdue apology to Lindsay, we always chose to blame his trackwork..sorry, Oldmate. (Some did, some knew better...Mike)
Work on the bogies has commenced with the front units hind bogie receiving attention. The lateral control springs from all four bogies should be in Sydney by the end of the week to be overhauled while the crew work on the bogies.