6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Jun 25, 2014
Jun 12, 2014
Sunday 18 May 2014
Today saw a number of things being attended to, one of which was the final fitting of the smokebox cover that covers the top of the front end throttle. This plate, which belongs to the original boiler and smokebox assembly, needed some work to get it attached properly. to achieve this, Malcolm, Ewolt and Greg spent most of the morning struggling with blunt drill bits and half charged batteries to drill the last few holes to hold the plate securely to the smokebox.
Malcolm managed to get himself into all sorts of weird positions in the smoke box between the super heater elements and the smokestack to push bolts up from underneath so that a nut and washer could be fitted from the outside... Needless to say that with the soot from recent steam tests and a bit of silicon to seal things up, the boys were just a little dirty as they moved onto the next task. Hopefully we wont have to take the plate off for a number of years. Andy was again toiling away on the electrical conduits in preparation for pulling cables in the next few weeks.
Sean and Mike and Howard were hard at work in the firebox, re installing the grate mechanism now that the ashpan was back on the loco. The job started easily enough, with parts passed into the firebox and returned to their proper positions, but the easy stuff was soon over and the linkages had to be refitted while lying on our backs in the ashpan, in doing so, we also removed the option of exiting the firebox the easy way, though the door. Pictures show some of the process of putting it back together. Once the mechanism was back together, the only exit available was through the bottom of the ashpan.
Alan and Malcolm returned the drivers side injector pipework that had been removed to make way for the ashpan and by lunch, that task was pretty much done. Sean was also seen working on new gaskets to seal the hatch on the rear tank, something you don't worry about on most steam engines, but very necessary on this one if you want to keep water in the tank on an incline.
Next up, the task of finding and eliminating air leaks was attended to... several were found under the cab floor, in almost inaccessible places. Some contortions and a few choice words later, Alan and Mike had eliminated the biggest ones and were now in search of smaller ones. By the middle of the week, Alan was able to pronounce the air system free of leaks, which was quite a milestone... The brakes now work, properly!
Saturday June 7
The list of outstanding job has been getting smaller every work day. With the initial static steam tests completed work is now focusing on the ash pan and the smoke box. The ash pan flushers had to be fitted and drilled in position to ensure the water would spray on the hot ash in the pan away for the fire bars. The skinny guys were selected as they could fit up through the bottom of the pan. Thanks to David and Malcolm, yep the skinniest guys in the team. A test for flushing was completed by hooking up the fire hose and all went well.
Ben and Alan reworked the ash pan spark screens and fitted new mesh to the fireman’s side. The final fit proved successful with all gaps in specification. A final coat of hi temperature all over black and it all looked as good as new.
The sand system small bore piping and last remaining sand pipes were fitted. This also included the install of the flexible hoses that run from the boiler cradle to the engine units. The six pipes were made all new utilizing the old end fittings.
The sand system tested well with only minor leaks detected and repaired. De sanding pipes now have to be fitted as mandated by network rules.
Steve Preston and Andrew Bridger commenced the install of the ICE radio with the configuration issues now sorted. Some new equipment boxes still have to be made and installed. Thanks to Andrew and Steve for the expert help and the long drives from home from Canberra.
The 60 class were never fitted with speed recorders but it is a network requirement to have one fitted. A search around the country and a cry for help has yielded a good result. The 60 class driving wheels are the same diameter as the Tasmanian M class and as luck would have it the Don River Railway has a spare speedo drive in stock. Thanks to Dennis Camplin and the DRR for making this vital gear available.
In terms of the overall project the rebuild of 6029 is now coming to an end. The compliance documentation has been submitted to the National Regulator and network owners for approval. At this stage and all being well the initial trials we commence in July. However the testing phase will take some months to complete. This will also include crew training and certification. Our affiliated RTO Go Train Industries have completed the operating manual and lesson plans.
As safety is our highest priority, the testing will be rolled out progressively in line with the approved risk assessments and network rules. A friendly reminder is extended to all interested observers and photographers that accessing the rail corridor without the appropriate authority is prohibited and in fact is viewed as trespass by the regulators. We encourage everyone to enjoy their hobby while acting responsibly and observing network rules. Representatives of the network managers will be present during our trials and are likely to challenge anyone within the corridor.
If you want to get up close and personal with 6029, Canberra Railway Museum is now open every day and 6029 will be on display when not operating so you are most welcome to visit and have an up close look.