The cold has hit Canberra; snow has reached the mountains
and frosts the windscreens of the cars. Of course not all is lost – the shortest
day passed last weekend and so have a few key milestones on the path to our
first inspection.
The wiring for the electrics has really been underway for
some time but the last week has seen some accelerated progress. As mentioned by
Alan we are rapidly approaching testing days and certification so, everything
needs to be ready. This has provided incentive to the electrical fitter, aka
Andy to deliver some critical steps in the wiring harness fit out. The critical
lengths of wire running from the generator to the main bus have now been
fitted. Previous wiring to head and tail lights already completed. The bus must
carry all power to charge batteries, run lights and fittings and also the
critical ICE radio. Clearly, most of this gear was never even dreamed of when
6029 was in the foundry being cast and beaten into shape. As a consequence
there are many electrical engineers and experienced people engaged to advise of
their needs for the specialty equipment and what power and voltage they need.
So Andy is running lots of thick cable down conduit that is narrow and
restricted – lubricant has been required.
The radio aerials and connecting wiring has been installed
on the coal bunker and the metal sides and ends for the radio and battery box
delivered.
Passing on from the electrical components we moved to the steam
side of things. The air compressor some may remember at Easter showed a lot of
leaks around the glands and the lubricator (for those with a good eye and
memory) seemed to stick at the 90 degree position in its rotation. So the compressor
was tested and pushed and shoved and finally it revealed its problems and spoke
by belching steam from a gasket. The low pressure cylinder was only generating
about 15 psi rather than 70 psi. This was causing the lubricator to fail –
simply not enough pressure! Secondly why was the pressure so low? The gasket
had blown and allowed steam and water to never fully move to the next stage of
the pump and the exhaust. This finally came to a head when the pump just
stopped and sent steam and water out through the gasket. A minor setback, but
better to happen now than later when we are out on the road. A new gasket will
be laser cut from the original drawings and all will be replaced.