Up to date information regarding the restoration of steam locomotive 6029 in Canberra, ACT Australia. Beyer Garratt 6029 is an EX NSWGR locomotive and was a member of the largest, and most powerful class in Australia. The restoration to full working order is being undertaken by volunteers in Canberra.
6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Apr 19, 2010
One Mans Shed
Something you will not have seen, is the amount of work he puts in at home, repairing and re-manufacturing parts required for the project. Take a look at the photos and you will see that his workshop is being put to very good use, and I think the we can all agree that his help is most welcome...
Thanks Ian, from everyone involved in the project!
Sunday 18th of April 2010
Sunday morning started with Paul setting up the power leads and air compressor lines in preparation of the day’s work. It was pleasing to see a good workforce turn up so the opportunity was taken to give the work site a good clean up . Kyle and John (the bogie boys) fitted the last of the brake components to the inner leading bogie. It is now safe to say that this bogie is now finished, well done guys only three to go.
Ian and Paul fitted the boiler cladding sheets to the fireman’s side of the fire box. The end product was a joy to behold as it was to Ian’s usual high standard. The boiler cladding sheets are being fitted before the boiler is lifted onto the cradle. This will allow the easy fitting of the injector starting vales and feed lines.
Marc, Peter, Josh and Howard worked on and around the leading engine unit. As usual bucket loads of grime and baked on cylinder oil gave way to the cast steel engine bead. The two leading sand boxes were removed and as suspected they were full of congealed 30 year old locomotive sand. As this problem was anticipated both were dried out on a pre prepared wood fire. One hour later the sand was easily drained and blown clear with compressed air. The removal of the sand boxes facilitated access to the two brake cylinders and both piston were stripped out for assessment. The cup seals were found to be in good condition and were cleaned down with the steam cleaner. The draft package for the leading engine unit was steam cleaned and will soon be painted in preparation for its final fit.
The above mentioned describes a series of parallel tasks that form part of the critical path plan. The work around the leading engine unit must take place before the two bogies are finally lifted into position. All being well the leading tank will then be lifted for its final fit. However to realise this major milestone we need your help now. No skills required just willing hands. To move things along we will be holding a two day work session. This will be the 30th of April and Saturday the 1st of May. All welcome.
So it’s all hands on deck as we are starting to put 6029 back together and we need your help now!
Alan Gardner