Up to date information regarding the restoration of steam locomotive 6029 in Canberra, ACT Australia. Beyer Garratt 6029 is an EX NSWGR locomotive and was a member of the largest, and most powerful class in Australia. The restoration to full working order is being undertaken by volunteers in Canberra.
6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
May 25, 2011
Sunday, 22 May 2011
The brake system is in general terms, continuing at a good pace but the cab sub floor piping requires significant work. So much so the it has been decided to replace the drivers side cab sub floor sheet for two reasons. The first being that it has seen better days and the second being access to a very cramped space. The floor was cut into two sections to allow the brake stand and sub assemblies to be removed for assessment and repair. The grimy, rusted pipes only yielded after we applied heat with the oxy torch helped by hydraulic jacks. The four feed valves and many smaller fittings are now off site being rebuilt as home work and yes they are seized and full of that rusty grime.
The cabs steel sub floor is about four inches below the timber floor and supports many sub assemblies including a myriad of pipes, both steam and air. Much of the rust and grime in the area is a direct result of coal dust and over use of the cab hose. Maybe the manufactures knew this as a this would ensure the purchase of new locomotives for future sales. Oh well bad timing you might say as diesels were well into production when 6029 was new!
Our next workday (Saturday June 4) will see us continue around the cab sub floor area. Hopefully the new replacement sheet for the sub floor will be on site ready for fitting by then.
Alan Gardner
Apr 19, 2011
Its been a while...
The cab has been riveted over 2 days, with help from Goodwin Alco's Steve Preston, Craig and Dave, along with the two Mike's and Malcolm. The days were very noisy, and it was good at the end of the day to see lots of bolts replaced by rivets. Photos will follow shortly.
In Canberra, the hind unit has again been getting some attention. There has been some abrasive blasting performed to clean up some areas, the rear draft package is back in, and I am sure that there has been more black paint applied wherever there was bare metal.
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The boiler has also been getting its fair share of attention, with the crinoline bands bing refitted in preparation for some new boiler cladding. More info shortly.
Mike
Mar 21, 2011
Sunday 20 March 2011
With the boiler in place, and after a quick check for clearance, the expansion slides were fitted in preparation for the expansion brackets. They could not be bolted down as some of the studs will have to be replaced. The exhaust steam ball joint that attaches to the blast pipe was checked and it comes as no surprise that some major surgery will be required.
After lunch some of the guys were treated to a ride around the yard on locomotive 1210. It was a pleasant change from eating grinding dust. With all that out of the way, the team started to piece together the remaining crinoline bands. As the name suggest these bits are the frame work that holds the cladding sheet metal in place. Some of the lower parts of the bands are rusted out so new sections will be made as required.
Looking forward, and the next few months should see the cab returned to Canberra for final fitting. With the boiler and cab in place the steam pipes and fittings will be hooked up for the eventual steam test. We are asking for everyone to make that extra effort and attend the next few workdays as the big move is on. Come April, we see 6029 shunted into the large shed to facilitate the fit out of the lubrication system, cab floor and anything else that needs doing. We will also need all hands on deck to help clean up the large shed before 6029 moves in.
Alan Gardner
Mar 20, 2011
Ok.... so we didn't expect this!
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From Boiler in |
Mar 8, 2011
Saturday 5 March 2011
The first job was to screw down the two large tension bolts that form part of the self adjusting pivots. They are designed to be pre-set at a tension which allows the pivot to self adjust for any wear. The adjustment of the screws required the combined effort of Paul, Tony and Andy utilizing four foot long pipe on the end of a four inch AF spanner. After about an hour of grunting and groaning both screws were at the required tension. For the record, a gap of 11/8" is called up on the manufactures drawing. The male pivots on both engine units had accumulated some minor surface rust and David soon cleaned off the offending iron oxide and applied a liberal coat of cylinder oil.
All this activity was leading to the project milestone of once again having the three major elements of the two engine units and the boiler cradle back together. Both the engine units were positioned to approximately the correct distance from each other. The boiler cradle was gradually lowered onto the engine unit’s, one end at a time. The end result of seeing the locomotive back together satisfied the crew to no end.
With the boiler cradle off the ground, the opportunity was taken to give the site an overdue clean up. The clean up will facilitate the long anticipated lifting of the boiler onto the boiler cradle. With only some minor prep work to complete it is anticipated that the boiler lift will take place in the next few weeks. This has only been made possible with the generous donations made recently by our project supporters, thanks to all who have contributed.
Our next workday is Sunday the 20th of March 2011
Alan Gardner
Mar 7, 2011
Stop Press
More info, and more pics very soon!
Feb 21, 2011
Sunday 20 February 2011
The hind units headstock and coupling area was stripped down for assessment but not before a nest of wasps were evicted from their home inside the casting crevices of the automatic coupling. The project manger was stung by one wasp who took exception to being moved out. After the wasps finally got the hint, Andy and Howard removed the coupling carrier plate, brake isolating cocks and with some persuasion, the automatic coupling. The short brake pipes from the isolating cocks to the first barrel unions will be replaced as they were in poor condition. The step on the right hand side of the head stock was straightened and repaired and in truth it has not been on the locomotive for many years. The damage sustained was due to a rough shunt many years ago. The hind unit draft package friction springs are being manufactured new by the local spring manufacture. Once the replacement springs are delivered the draft package and automatic coupling will re-fitted to the hind unit headstock.
Now that the bogies are in place the "A" team of Kyle and John completed the fit out of the brake and flexible hoses connecting to bogies to the engine units. Some of the pins and bushes on the brake hangers were replaced as the team was not happy with the sloppy fit. The flexible lube lines received a final visual inspection and as predicted all were in the correct place and are a good fit.
As a direct result of today’s work, we are now in a position to start planning the lowering the boiler cradle onto the engine units. Both pivots will be preset in accordance with the manufactures drawings. The pivots will be cleaned for the last time and then on goes the boiler cradle. We can now move onto this vital stage as we have recently received a significant donation from some of our supporters. Thank you to everyone who has contributed and because of your efforts, the next couple of months will see 6029 back together in three distinct pieces as an articulated locomotive. This will make the way clear for lowering the boiler into the cradle in the next month.
So its all go systems go for some exciting times ahead.
Keep steaming
Alan Gardner
Feb 7, 2011
Saturday February 5 2011
Andy and Tony started the clean up around the hind engine unit and cylinders in preparation of the installation of the forth bogie. As predicted bucket loads of baked on cylinder oil and road grime are prevalent and we expect quite a few hours of toil here. The next couple of workdays should see this task completed with only the bogie to roll under.
As the bogie work is all but completed the boiler cradle leading pivot was the next job on the list. Graeme and Shaun fitted both halves of the very large bronze pivot castings. The reconditioned tension spring nuts were screwed down to the pre-set clearance. While we were working on the leading pivot, Marc and Paul removed the live steam ball joint that is situated just above the pivot casting. The two lube lines that supply oil from the mechanical lubricators were found to be completely broken off. The cavity that the ball joint sits in was completely block solid with congealed oil and again lots of crud was cleared away. Needless to say, the lube lines will be repaired to the usual standard and maybe the oil will again be delivered to where it is required.
The good news is that we are now almost ready to start the reassembly of the engine proper. The first job will be to lower the boiler cradle into position followed by the boiler soon after. Having said that, we now need to raise the funds to facilitate the crane hire. We are asking for everyone to chip in and in fact, $3,000 will see the mighty 60 class starting to look like the real deal again.
Our next workday is Sunday the 20th of February and if we get a good turn out of volunteers we will be almost ready for the big reassembly.
Alan Gardner
Jan 18, 2011
16-17 January 2011.
The object of the weekend was to install the third bogie(hind inner) under the hind unit. Andy and Tony continued to clean up the hind unit bogie pivot and sub assembles to facilitate the final fit of the bogie in question. No surprises here except for more coal fines in the frame casing cavities. This area directly below the coal screw conveyer and bunker so we guessed that there may have been some overflow when 6029 was being filled up for its runs. The final fit out of the bogie consumed significantly more time than we estimated as the project manger couldn’t work out the difference between left and right. As a result of this three attempts were made to fit the pedestal keep plates, third time lucky hey!
Paul stripped down the hind unit draft package(the big spring that absorbs the in train buffing forces) on the hind unit and as usual more road grime was present. The bottom retaining plate holding the draft package in place was cleaned down and crack tested with no issues identified. However the ¾" nuts were almost non existent from the effects of rust...Replacement nuts and bolts have now been ordered.
At 16:00 hrs on Sunday the inner hind bogie was lowered into position will little bother or fuss although the hot and tired crew were ready for a well earned drink and pat on the back.
Alan Gardner
While this was happening in Canberra, the cab was again receiving attention at Eveleigh, with more new panels being fitted. In one of the best turnouts we have had for a long time, Mike, Mike, Ron and Malcolm were onsite for the day. Lots of hands made light work, allowing the new roof panels to be trial fitted and they are a surprisingly good fit. The roof is made in three sections and are yet to be trimmed and welded together, but there is most certainly light at the end of the tunnel.
By the end of the day, all the panels that make up the sides of the cab had been refitted and we had even managed rehang a door with new hinges...It wont be long now and we can rivet it all back together.
Jan 11, 2011
What happens when an armament fitter gets interested in steam?
He has transformed the old, neglected lubricators into what I suggest is easily better than new condition.
Have a look at the before pictures, and compare them with the after... You will see what I mean! And then look at how complex they are... Every output is an individually metered, self contained pump, and Ian has rebuilt every one...
Well done Ian!