6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org

Mar 8, 2011

Saturday 5 March 2011

The first day of spring realized mild temperatures that were a welcome relief from the summer heat. The day started with the usual drill of running out of the power leads and a cup hot strong coffee.

The first job was to screw down the two large tension bolts that form part of the self adjusting pivots. They are designed to be pre-set at a tension which allows the pivot to self adjust for any wear. The adjustment of the screws required the combined effort of Paul, Tony and Andy utilizing four foot long pipe on the end of a four inch AF spanner. After about an hour of grunting and groaning both screws were at the required tension. For the record, a gap of 11/8" is called up on the manufactures drawing. The male pivots on both engine units had accumulated some minor surface rust and David soon cleaned off the offending iron oxide and applied a liberal coat of cylinder oil.

All this activity was leading to the project milestone of once again having the three major elements of the two engine units and the boiler cradle back together. Both the engine units were positioned to approximately the correct distance from each other. The boiler cradle was gradually lowered onto the engine unit’s, one end at a time. The end result of seeing the locomotive back together satisfied the crew to no end.



With the boiler cradle off the ground, the opportunity was taken to give the site an overdue clean up. The clean up will facilitate the long anticipated lifting of the boiler onto the boiler cradle. With only some minor prep work to complete it is anticipated that the boiler lift will take place in the next few weeks. This has only been made possible with the generous donations made recently by our project supporters, thanks to all who have contributed.

Our next workday is Sunday the 20th of March 2011

Alan Gardner

Mar 7, 2011

Stop Press

It will come as a surprise to some, but Saturday saw the boiler cradle reunited with the loco units... More info soon, but certainly a milestone, and a sign of big things to come... Plus, not a mention of bogie's, well OK, just one!

More info, and more pics very soon!

Feb 21, 2011

Sunday 20 February 2011

4-8-4 + 4-8-4. Theses numbers may not be significant to an bystander but to the 6029 team it is a significant milestone. After 14 months of hard dirty work we rolled under the last of the four bogie. As we are now proficient with Garratt bogies an initial trail fit took place to double check for clearance and alignment . A wise decision, as we found a problem with the bogie in place. The two outer driving wheels had no contact with the rail head by about 25 mm. Further investigation revealed that the brake adjusting pull rods were not backed off and consequently the brakes where holding the driving wheels clear of the rail. Both four inch AF adjusting screws were backed off and on the second lowering the wheels settled back in the correct orientation. Sighs of relief all round and the crew was very happy to step back an enjoy the fruits of their labor.



The hind units headstock and coupling area was stripped down for assessment but not before a nest of wasps were evicted from their home inside the casting crevices of the automatic coupling. The project manger was stung by one wasp who took exception to being moved out. After the wasps finally got the hint, Andy and Howard removed the coupling carrier plate, brake isolating cocks and with some persuasion, the automatic coupling. The short brake pipes from the isolating cocks to the first barrel unions will be replaced as they were in poor condition. The step on the right hand side of the head stock was straightened and repaired and in truth it has not been on the locomotive for many years. The damage sustained was due to a rough shunt many years ago. The hind unit draft package friction springs are being manufactured new by the local spring manufacture. Once the replacement springs are delivered the draft package and automatic coupling will re-fitted to the hind unit headstock.

Now that the bogies are in place the "A" team of Kyle and John completed the fit out of the brake and flexible hoses connecting to bogies to the engine units. Some of the pins and bushes on the brake hangers were replaced as the team was not happy with the sloppy fit. The flexible lube lines received a final visual inspection and as predicted all were in the correct place and are a good fit.

As a direct result of today’s work, we are now in a position to start planning the lowering the boiler cradle onto the engine units. Both pivots will be preset in accordance with the manufactures drawings. The pivots will be cleaned for the last time and then on goes the boiler cradle. We can now move onto this vital stage as we have recently received a significant donation from some of our supporters. Thank you to everyone who has contributed and because of your efforts, the next couple of months will see 6029 back together in three distinct pieces as an articulated locomotive. This will make the way clear for lowering the boiler into the cradle in the next month.

So its all go systems go for some exciting times ahead.

Keep steaming

Alan Gardner

Feb 7, 2011

Saturday February 5 2011

The last of the four bogies was the main focus of the days work. The team fitted the flexible lube lines in time for Ian to deliver the next two sets of Nathan four way lubricators. The completed bogie was then transferred behind the trailing engine unit in preparation for its installation. We had to pinch ourselves...yes we were there, all done. All four bogies are ready to grace the network metals again, well done team. The opportunity was taken to complete some long overdue housekeeping around the space occupied by the bogies for the past year.



Andy and Tony started the clean up around the hind engine unit and cylinders in preparation of the installation of the forth bogie. As predicted bucket loads of baked on cylinder oil and road grime are prevalent and we expect quite a few hours of toil here. The next couple of workdays should see this task completed with only the bogie to roll under.

As the bogie work is all but completed the boiler cradle leading pivot was the next job on the list. Graeme and Shaun fitted both halves of the very large bronze pivot castings. The reconditioned tension spring nuts were screwed down to the pre-set clearance. While we were working on the leading pivot, Marc and Paul removed the live steam ball joint that is situated just above the pivot casting. The two lube lines that supply oil from the mechanical lubricators were found to be completely broken off. The cavity that the ball joint sits in was completely block solid with congealed oil and again lots of crud was cleared away. Needless to say, the lube lines will be repaired to the usual standard and maybe the oil will again be delivered to where it is required.

The good news is that we are now almost ready to start the reassembly of the engine proper. The first job will be to lower the boiler cradle into position followed by the boiler soon after. Having said that, we now need to raise the funds to facilitate the crane hire. We are asking for everyone to chip in and in fact, $3,000 will see the mighty 60 class starting to look like the real deal again.

Our next workday is Sunday the 20th of February and if we get a good turn out of volunteers we will be almost ready for the big reassembly.

Alan Gardner

Jan 18, 2011

16-17 January 2011.

Our first workdays of 2011 got off to a good start as for once it wasn’t raining in Canberra. Large puddles of water were still prevalent but at least the forecast was for a fine and sunny weekend.

The object of the weekend was to install the third bogie(hind inner) under the hind unit. Andy and Tony continued to clean up the hind unit bogie pivot and sub assembles to facilitate the final fit of the bogie in question. No surprises here except for more coal fines in the frame casing cavities. This area directly below the coal screw conveyer and bunker so we guessed that there may have been some overflow when 6029 was being filled up for its runs. The final fit out of the bogie consumed significantly more time than we estimated as the project manger couldn’t work out the difference between left and right. As a result of this three attempts were made to fit the pedestal keep plates, third time lucky hey!



Paul stripped down the hind unit draft package(the big spring that absorbs the in train buffing forces) on the hind unit and as usual more road grime was present. The bottom retaining plate holding the draft package in place was cleaned down and crack tested with no issues identified. However the ¾" nuts were almost non existent from the effects of rust...Replacement nuts and bolts have now been ordered.

At 16:00 hrs on Sunday the inner hind bogie was lowered into position will little bother or fuss although the hot and tired crew were ready for a well earned drink and pat on the back.

Alan Gardner


While this was happening in Canberra, the cab was again receiving attention at Eveleigh, with more new panels being fitted. In one of the best turnouts we have had for a long time, Mike, Mike, Ron and Malcolm were onsite for the day. Lots of hands made light work, allowing the new roof panels to be trial fitted and they are a surprisingly good fit. The roof is made in three sections and are yet to be trimmed and welded together, but there is most certainly light at the end of the tunnel.



By the end of the day, all the panels that make up the sides of the cab had been refitted and we had even managed rehang a door with new hinges...It wont be long now and we can rivet it all back together.

Jan 11, 2011

What happens when an armament fitter gets interested in steam?

Ian Senini has outdone himself with his latest project.... Take a look at the wonderful job he has done on the mechanical lubricators for the Garratt!
He has transformed the old, neglected lubricators into what I suggest is easily better than new condition.



Have a look at the before pictures, and compare them with the after... You will see what I mean! And then look at how complex they are... Every output is an individually metered, self contained pump, and Ian has rebuilt every one...

Well done Ian!

Dec 29, 2010

What is the best way to find something you have misplaced?

At the last work day, it was found that spacer that is part of the lateral control assembly could not be found... Now I ask you... What is the most reliable way to find it?

Make a new one! And that is exactly what has been done. Al had a new one made a day or so after the last workday, so we can be sure that the original will be staring at us the moment we finish the assembly of that last bogie... Murphy's law pretty much guarantees it!

Dec 22, 2010

Sunday 19 December 2010

Following on from the efforts of the team at Eveleigh on Saturday the guys at Canberra started bright an early for the last workday of 2010.



The leading engine unit was once again lifted to allow the leading inner bogie to be rolled out clear. Four new ¼-½ inch BSP nipples were fitted to replace the worn out brass type. A trial fit of the flexible hoses confirmed all was well with the grease lubrication system to this bogie.

New replacement packing plates for the centre pivot bowl had been ordered in the past week and were on site ready for fitting. It was decided to replace the old 3/8 liner with the same as we may have vary the packing when the locomotive is being weighed. After the packing was in place, the composite low friction liner and locking ring was installed with an easy tap in fit. With a final check of all clearances the bogie was rolled into place and the engine unit was lowered into place with all being well. The flexible grease pipes were installed and fresh grease pumped through. The four inch diameter king pin was lowered into place, the locking plate and split pin fitted and finally we could say job done. Now onto the hind unit! Thanks to Paul Nowland, Graeme Kidgell, Shaun Barker and Marc Miller.

Pater Reynell washed down some of more gummed up components of the hind unit. This is in preparation for the removal of the hind unit draft package. The draft package is directly behind the headstock and is attached to the shank of the coupling. In essence the draft package absorbs most of the in-train buffing forces and from past experience we expect hours of fun here. When Peter has finish with the external clean up of the hind unit, the draft packaged will be dropped out for full inspection.

The day came to a sudden end at 13:30 hours as the rain set in for the rest of the day. Yes the joys of working out doors.

Alan Gardner

Dec 19, 2010

Saturday 18th December, Cab Progress

The last workday for 2010 at Eveleigh saw a lot of progress, yes, a lot! Just the two Mikes(Reynell and Ridley) got stuck in to it and the pictures show what can be done when a plan starts to come together.

First order of the day was to build a frame to support the entire cab and to hold everything square. You can see from the pictures that the frame is more than a few sticks of timber. The frame will remain attached to the cab until it is reunited with the boiler cradle.Once square and rigid, the work became much easier as it was much easier to create the required reference points and to reattach each component.



Some more parts were collected from our old mates at R&L Wall in Lidcombe on Friday and today saw them all fitted without too much problem. The new rear quarter panels still require a bit of bending, and a few pieces welded in, but overall, everything went together very well and it was well worth the effort of replacing the badly damaged panels.

You may also notice that the spectacle plates have been replaced. The old ones had suffered badly in places, as had most of the cab. Full points must go to Ian and Chris from R&L Wall, as they not only made the new ones, but also did an amazing job of saving all the fittings from the old panels without damaging any..... Thanks Chris!

There will be little adjustment required to the panel above the fireman's window as well, a problem that was only revealed as the surrounding panels were reattached. No problem however, as the generous application of heat and a swift whack from a large hammer should see the problem corrected at the next workday.

The next workday should see all the panels in their final positions and the cab ready to be riveted as required.... Now wont that be nice!

Mike Reynell

Dec 8, 2010

Saturday 4 December 2010

The leading engine unit is now staring to look like a complete locomotive. Andy Hays and Howard Moffatt spent a few hours going over the last bits of the grey primer. The trailing end of the leading unit was given a final coat of black in preparation for the fitting of the leading inner bogie. This bogie has been finished for some time now, but could not be fitted as a new centre pivot bush was being manufactured. The new bush was completed by a contractor early on in the week. The female pivot on the bogie was full of water due to Canberra wet spring and as a result of this some surface rust had to be cleaned off before the bush could fitted. Lachlan took out the water and cleaned out the surface rust. The bush was fitted with a good size for size fit and some long tack welds were also applied to ensued that the bush will remain properly fitted. The leading engine unit was lifted and the bogie rolled into place with no issues. There is nothing more pleasing when a plan comes together like clockwork.



Andrew Bridger and Graeme Kidgell continued with the strip down and assessment of the hind unit valve gear and motion. It all looks to be in good condition but the years of grime will see endless hours of polishing.

From an overview perspective the fitting of the last two bogies to the hind unit will be the top priority but before this can take place, many components that the bogies stop access to will have to be addressed. Items such as the coupling and draft gear will have to now be dropped out. Hey haven’t we done this before, oh yes....its a Garratt. Twice the loco and twice the fun!

Alan Gardner