Up to date information regarding the restoration of steam locomotive 6029 in Canberra, ACT Australia. Beyer Garratt 6029 is an EX NSWGR locomotive and was a member of the largest, and most powerful class in Australia. The restoration to full working order is being undertaken by volunteers in Canberra.
6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Sep 23, 2009
Sunday 21 September 2009
Mike Reynell delivered the steam pipe spacing rings made by an external contractor in Sydney. These rings will
facilite the fitting of the insulation and cladding to the main steam pipe that runs down the right side of the boiler cradle to the hind engine unit.
The front end throttle overhaul is being completed by Mike Reynell at his Sydney works. Mike showed off his handy work with the completed repair of the throttle shaft. He is now focusing on the main vales and associated fittings. Ian has also been beavering away at home with the last of the backhead sheets and he advises that the final fit is only days away. His biggest issues has been the neighbours washing and the over-spray drifting over the fence.
The re-assembly of the first bogie continued with the repaired manganese liner’s fitted. The brake equipment for this bogie was assessed and re-painted for eventual fitting.
Our next work day is Saturday the 3rd of October. Work will again focus on the bogie rebuilds.
Alan Gardner
Sep 7, 2009
Saturday 5th September
The second of the four bogies was rolled clear of the hind unit and as expected it resisted all of the way. The locking pin that retains the king pin was completely seized and several attempts to remove it was unsuccessful. As a consequence of this a large part of the morning was dedicated to the cleaning out of the hollow passages in the main frame casting. This allowed access to the locking pin assembly inside the main farm. After we extracted bucket loads of coal and gunk we could at last see the seized locking pin. The usual heating with the oxy torch did not seem to do much and it was looking like a "too hard" scenario would prevail here. However to our surprise, with several blows of the sledge hammer the pin stated to move. After we extracted the locking pin the King pin dropped straight to the ground without fuss. Half an hour later the bogie was clear of the hind engine unit. As can be seen in the photos years of grime will have to be removed before disassembly can take place.
The first bogie that was removed last month now sports its second coat of black paint. All of the components are progressively being repaired and painted. Our next few workdays should complete this bogie with significant progress on the second one. It is anticipated that the last two bogies will be relatively quick to complete as they do not have brake gear fitted.
Our next few workdays will focus on the bogies and when competed the re assembly stage of the project will start in earnest. However we still need your help either financially or in person. Our next workday is Sunday the 20th of September and could I please ask that you take the time to come along and help. Lunch is provided!
Alan Gardner