Up to date information regarding the restoration of steam locomotive 6029 in Canberra, ACT Australia. Beyer Garratt 6029 is an EX NSWGR locomotive and was a member of the largest, and most powerful class in Australia. The restoration to full working order is being undertaken by volunteers in Canberra.
6029 is owned by the Australian Railway Historical Society, ACT Division and the restoration is proudly supported by their tourist operations and by the generous donations of members and public supporters.
The society operates rail tours out of Canberra with our heritage fleet of steam and diesel locomotives and rolling stock every few weeks.
To travel in style on any of our tours, or to learn more about our collection and operations, go to Canberrarailwaymuseum.org
Nov 16, 2013
Project 6029 Updates 3rd October to 2nd November
Oct 3, 2013
A note for anyone who was going to attend the next workday...
Sep 18, 2013
PROJECT 6029 Update 17 & 18 August and 7 September
Now where were we... There were some areas mentioned previously about sunshine and darkness requiring painting. First order of the day was cleaning the area to be painted – the area is of course under the hind tank and bunker in the spots meant to be painted when there is no tank in place. As all painters will tell you preparation is the key to a great job, so it was back to scrapping and wire brushing. Angle grinders with wire wheels can be quite frightening at the best of times, but when they take off or veer off course while held at the extreme limits of your arms’ length they can be quite different. All this whilst performing the act in a confined space that would make the average contortionist proud and it probably should be listed in the top ten positions in the Karma Sutra! We achieved about fifty percent of the area scrapped and primed ready for the top coat. Next work detail will see the other side scrapped and primed.
Aug 12, 2013
Saturday 3 August
Jul 24, 2013
Update for the weekend 20 & 21 July
After what felt like the coldest start in the project's (selective) memory we got off to a steady flow of work. The first task was....Get that grate finished, so OK, down to it - locate all the holes for the grate mounting brackets, confirm they were the correct ones and carefully tap them out. The tap costs $75.00, so caution was a large part of the initial approach, however after getting used to the equipment, the speed of tapping could increase. Sixteen holes were tapped and two were adjusted and given over sized threads to handle the affects of wayward drilling. Try drilling upside down for a few hours and you understand why some holes were slightly off centre.
The brackets were all arranged and bolted home except for one stubborn one that ultimately needed drilling out to a larger diameter. There are four brackets running along the foundation ring on each side of the firebox. These hold in place two long iron castings that can only be described as long, with four semi-circle cut-outs along the top and look like instruments of torture if they were not so heavy. Essentially these elements hold cross bars that are half the width of the firebox and are supported at the semi circle cut outs on the foundation ring side and in the middle by the main longitudinal central brace. There are eight down each side. The rocking mechanism allows the grate to be divided into four sections and each section to be operated independently or together. An easy way to picture it is in plan view looking down. It is a grate made up of 8 cross pieces of two bars each supported by a central beam and on the outside by 4 beams end to end, two on each side. Better still come down and stick your head under the firebox and you will get the picture. Anyway, at quitting time the foundation of the grate was ready for the next days team to assemble and complete the rocking grate.
While there was patient murmurings going on under the firebox the dulcet tones of the rattle gun and some human words of encouragement (or were they threats?) were coming from on top. Yes the blower valve assembly, gland packing and assorted bolts were being put in place. Access was limited and angles were not easy, but none the less, success was ours and the blower valve mechanism was hooked up to the reach rods running from the cab on the driver?s side. All works as it should... off and on. All we need now is some steam!
Oh, and lets not forget the all important valve assembly and those pins... we'll get back to you on that. Seems our fabricator has lost the order for the last 6 pins. So we are awaiting these. Who would believe these could be on the critical path? We will update as soon as they arrive and are in place.
So as daylight faded on Saturday afternoon, we left 6029 with half the supports for the grate in place, and a blower valve operational and ready for testing. Excitement is building, anticipation and again the sense that it is very close now........
The Waugh rocking grate is American by design and was standard equipment in most US coal burning locomotives after the First World War. The design has no fixing other than the mounting plates and the middle main girder that attach under the fire box foundation ring. The rest simply falls into place starting with the support girders with the U shape pivots running either side of the fire box. 16 pivoting rocking bars drop into the U shape pivots and last but not least, 304 finger fire bars slot in to place. Easy...
The NSWGR specified this type off fire grate for the 60 class, and in fact it was standard to all new coal burning locomotive during the 1940's and 50's .
Wet drizzle and cold conditions greeted the Sunday crew at first light. Lucky for 6029 she now resides undercover in the main display shed at the museum.
The first job of the day was to fit the last two brackets that hold up the main support beams of the Waugh rocking grate. The rattle gun was put to good use as the crew tightened up the last of the nuts. After that the team set up a chain gang and yes, all the bits just dropped into place. The majority of the work could be completed from underneath but the last element had to be dropped into place from inside the fire box.
The reversing wheel assembly was one of the many smaller components that were out sourced to smaller workshops. It was delivered and fitted by Bruce and Keith from Sydney. It was pleasing to see the last of the cab components now fitted into place. Bruce also fitted the cylinder drain cock assemblies to each of the four cylinders. This is a small air driven cylinder that is fitted with a spring to keep the drain cock open. Compressed air is used to close off the drain valves when in operation.
The fitting of the fire grate is a significant milestone and in fact puts the project on track for that all important first fire. All tasks will now centre around the fitting of smaller components and operational testing.
Our next work day will see 6029 shunted out of the shed to fit the stoker motor and associated pipe work. We are calling for all hands on deck for the next few workdays as we are very close to that all important first match.
Oh, and last but not least, our friends at Goodwin Alco delivered some new builders plates, to replace the long lost ones. The new ones were cast from a replica plate made by the late Arthur Reynell in the '70's from printers lead.... A lick of paint and they will look brilliant...
Jul 13, 2013
Saturday 6th of July
Jul 3, 2013
All Hands On Deck
Alan has asked that anyone available comes this Saturday the 6th, as more hands make lighter work, and there is little heavy lifting to do.... Its time to refit the fire grate, and we need some bodies to lift the iron support casting back into position. The more people who turn up, the greater chance we have of getting it back in position and in turn, the rest of the grate mechanism can then be re-fitted.
So if you can make it on Saturday, come along and help, The younger and fitter the better, but hey, more hands make lighter work, and sometimes, even moral support will help, so brave the cold and lend a hand...
Jun 11, 2013
1 June, 2013
A good turn out meant once again key tasks that needed technical skills could be commenced. The first was installing the support brackets for the coal bunker at the cab end. These brackets mount to the frame on the front of the hind engine and then to the front of the bunker. They required welding and grinding to be accurately put in place. Thanks Mark for your skills in this area. Next work day will mean this can be completed and that task can be put in the “done” list.
Andy and Toby continued to work on the coal trough and associated running gear – they have worked tirelessly on the auger trough and bunker now for many weeks. There are many bolts and mounts to align for the coal trough and auger to ensure it mounts properly to the frame. The talents of a contortionist and the hydraulic ram to make things align have come in handy. The space is quite difficult to access and is quite literally in the bowels of the bunker. Their work progressed well during the day – see the associated pictures for details and how tight some of the places they are working in really are!
Polishing of the connecting rods and valve linkages continues as these require constant work to maintain. Our newest recruit, Ewoult,
May 14, 2013
Project 6029 Update 4 May, 2013
The autumn days are proving to be a great bonus to the team – cool sharp mornings with
plenty of sun shine and mild temperatures during the day.
The team gathered early as there had been a rumor that the cylinder covers had been
removed from the lead engine. And the team were impressed! During the week Alan and
with the some assistance of James Simper had removed the covers from the right front
cylinder and valve housing to reveal a delightful sight – grease! And no rust. Mike Potter
removed the pistons and piston valves for storage many years ago had done a great job in
sealing the cylinders to prevent corrosion. Not even possums had got in!
The right front was soon removed and it also revealed – yep grease!
So far the front left cylinder on first preliminary measurements is showing a diameter that
is within tolerances – there is only a few thou or so available. Good news. That is a good
omen for the remaining 3.
Speaking of omens this is the second work day in a row that a new team member has
come along to assist. In addition there were 7 plus Alan and Sean (lets not forget Jack
too) to get stuck into some of the work. A large number of people saw some excellent
progress.
The casing (oyster is the name that describes this clam shaped object) around the
universal joint that allows a flexible join between the stoker auger in the tender to the
auger under the cab was checked and cleaned. Roger replaced some well corroded studs
and cleaned an area up on the housing that required welding. Alan completed the task and
the housing was finished off with some regulation black paint. More on this house later.
The tender received 3 main pieces of work. Our new member James, being a qualified
welder provided much needed skills to heat, bend and weld an after market plate that the
NSWGR had bolted to the cab end of the coal bunker. This plate and one on the other
side are essentially spacers between the two cast saddles that support the tender at the
cab end by attaching to the plates and to the frame. The saddles will be installed shortly
after some essential parts are placed in the space between the frame and the bunker – that
oyster mentioned earlier, the stoker motor and the usual spaghetti junction of oil, water
and steam pipes and lets not forget the reversing reach rod for the hind engine.
Andy, ably assisted by his apprentice, Toby was making good the 20 odd bolts that join
the coal bunker to the auger trough. These bolts were well and truly “stuffed” when
we disassembled the unit so Andy and Toby have their work cut out sourcing bolts and
reaming out the holes. If you look closely at some of the pictures of the coal bunked side
on behind the cab you may see a series of what looks like short vertical tubes. These are
the surrounds for the bolts that Andy and Toby are working on.
Toby also continued painting the top deck of the coal bunker/tank at the rear of the unit.
Never and easy job that is necessary but was still well done.
Some 8 of the 20 odd mounting bolts were inserted and tightened on tender unit.
Critically these are spring loaded to the frame making a semi flexible union between
the tender and the frame. Strangely the bolts and springs are never the same length and
this meant squeezing each spring to allow the washer and nut to be threaded onto the
bolt. These are tough short springs that are not easily compressed. There are a number of
springs missing or broken so the remained bolts will await their arrival before completing
this task.
Moving towards the front of the boiler the smoke box and connecting pipes from the
compressor were cleaned, polished and painted and then the exhausted was stuffed with
sound deadening material and prepared to be attached. All hands, oxy, grinders and
gentle persuasion as is characteristic of the team meant this task took 4 of us to complete
– but it was done!
Lastly the taper pins for all the rods have been ordered and these should arrive shortly.
The last troublesome pin (LH1) which joins the radius rod to the reversing lifting arm
on the driver’s side hind engine was polished enough with emery paper to be able to be
reinserted in its mount. This means that we can on arrival of the taper pins complete and
sign off the valve gear and connecting rods – what could possibly go wrong?
Lastly the weekend saw more polishing and protecting and painting of more of the cab
light fittings and junction boxes.
Of course the day could not be complete without trying to assemble “the Oyster”. This
clever housing surrounds a universal joint that joins the bunker auger to the cab auger.
The latter is inclined steeply to pass under the cab floor. Naturally this required some
manual lifting to persuade the two augers to be rotated then extended back from the cab,
up an incline and aligned so a bolt could be inserted into the universal joint – get the
picture? Awkward and heavy. But done! Apparently the auger when working is so noisy
it rivals the rest of the engine in decibels!
Next we needed to extended the casing covering the cab auger back and up to align with
that oyster – given the time of day and the weights involved we determined that more
careful planning of the lift and the use of power jacks would be wiser – so we retired for
an evening beer instead.
Now for a treat... From the archives of Howard Moffat, here are some images from time long since passed, and often forgotten.
A great day’s work from all and pleasing to see some major tasks started and others
nearing completion.
Apr 25, 2013
PROJECT 6029 Update for the weekend of 20 April
Task one for the day was to continue drilling out and inserting new studs into the foundation ring of the boiler. As many may remember the boiler we are using is not 6029’s original boiler and it had received a number of modifications in its previous life. This meant that the original studs had been removed and/or cut off. As you may expect, there are a large number of studs that need to be replaced and doing this requires you to lie on your back and then drill out the studs above our head. Andy has worked out he gets the best results by using 3 stages of drilling and one of threading to make good each stud – how many are there to do? At time of going to press, this is a number greater than 10 and most likely closer to 30. Does someone want to guess? Even better, does someone want to help? There are few who can say they have laid under a Garrett and survived! Seriously, this task is important and if you would like to show off your ability to accurately drill heavy metal please come along and have a go. We cannot fit the grate or ashpan to the boiler until this task is completed.
The generator was also carried out of the shed and lifted into place beside the boiler on the fireman’s side. Given the Garrett was in the shed and as usual parked in a very inconvenient location, this meant an awkward manual lift was needed for a very heavy and odd shaped object. Fortunately the generated landed on its mounts correctly and safely. Alan and Howard located bolts and tightened it down.
The water pipe elbow mounted on the base of the rear tank was attached. It attaches on the driver’s side midway between the middle two driving wheels and presented another awkward lift but no where near as heavy as the generator. Made of brass it was rattle gunned into place on the tank and then joined to the water pipe leading forward to the injectors.
All valve rods have now been joined. This meant that checking and correct placement of the locking split pins could proceed. Each engine was approached with four pairs of eyes, each pin and its locking pins was assessed and noted (there are 8 pins with two locking split pins on each engine). Additionally, locking pins and nuts on the connecting rods were reviewed and checked. Missing grease nipples and split pins on the connecting rods were also identified and any split pins missing on key components were noted – the mounting brackets for the outer bearing of the expansion link being one of these items. We need 24 new locking split pins to complete the correct locking of the rods. There is great satisfaction in seeing these pins and rods joining up again. Its going to be satisfying shortly to be able to say to anyone that you worked on those shiny spinning rods – if you want to be able to say that please come along and have a go with a grease gun, spanner or an angle grinder polishing them. There are not many days left before we sign off the rods to our project manager for inspection!
Again spread the word that we need small or big change for those piston rings, we need to be able to pay for them before we order them, I am sure you can imagine that rings around 20" diameter do not come cheap. The rings are the last major milestone/hurdle for the project. Also, and this is a long shot, but if you have access to a CNC lathe or know someone who does, and would like to be able to that you contributed to the project, we need to get about 40 tapered pins produced. They are not particulary large or difficult to produce, being about 4" long, but they do need an accurate taper, so give it a thought... If you can slip a foreign order through at work, or you are lucky enough to have a CNC lathe at home, put up your hand and help us out. Drop me a line if you think you can help... mike@project6029.com